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ergoCub 1.2 S/N:002 – All torso joints in HF with generic motor error #1804

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carloscp3009 opened this issue May 8, 2024 · 2 comments
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ergoCub 1.3 S/N:002 ergoCub1.3 platform

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@carloscp3009
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carloscp3009 commented May 8, 2024

Robot Name πŸ€–

ergoCub 1.2 S/N:002

Request/Failure description

We were conducting some test on the robot that implies walking with a payload (Empty box) after a minute the robot went in Generic Motor Error in all torso joints.

torso_motor_fault.mp4

Detailed context

Here an screenshot from the motor GUI

image

This time the motor currents and PWM for the torso seem to be streamed correctly.
image

Additional context

Here the mat file containing the logging data:
robot_logger_device_2024_05_08_11_47_17.zip

And here the yarprobtinterface:
interface_generic_motor_error.txt

How does it affect you?

We have some demos the next week and a video shooting, without crane, tomorrow

cc @GiulioRomualdi @DanielePucci @S-Dafarra

@carloscp3009 carloscp3009 added the ergoCub 1.3 S/N:002 ergoCub1.3 platform label May 8, 2024
@github-actions github-actions bot changed the title All torso joints in HF with generic motor error ergoCub 1.1 S/N:002 – All torso joints in HF with generic motor error May 8, 2024
@valegagge
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Hi @carloscp3009 ,
from the log you attached it seems there are some CAN bus errors.

image

In addition, I noticed that there was a calibration fault on joint 4 of the right leg.
The calibration file you used is the one that is on the devel branch of the robotology?

cc @AntonioConsilvio

@AntonioConsilvio
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Hi!

Thanks for the suggestion @valegagge.

You are right, in fact the problem was caused by the CAN termination resistor not making good connection.

@AntonioAzocar and I fixed this problem, the robot works properly now!

Thank you!

cc @carloscp3009

@AntonioConsilvio AntonioConsilvio changed the title ergoCub 1.1 S/N:002 – All torso joints in HF with generic motor error ergoCub 1.2 S/N:002 – All torso joints in HF with generic motor error Jul 17, 2024
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Labels
ergoCub 1.3 S/N:002 ergoCub1.3 platform
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