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ergoCub 1.1 S/N:001 – Right Arm Elbow Encoder Reading Wrong Values #1810

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SimoneMic opened this issue May 14, 2024 · 1 comment
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ergoCub 1.1 S/N:001 ergoCub1.1 platform

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@SimoneMic
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Robot Name 🤖

ergoCub 1.1 S/N:001

Request/Failure description

While using the robot, the right elbow went in HW fault caused by the error: AEA encoder invalid data
While manually moving the joint we have seen erratic encoder values.

Detailed context

Here's the log of the error:

[ERROR] from BOARD 10.0.1.3 (right_arm-eb3-j2_3) time=725s 661m 46u :  MC: AEA encoder invalid data. Hardware problem in the magnetic position sensor of the joint caused invalid position readings. (Joint=r_elbow (NIB=1), encoderPort=0)
[ERROR] setReferenceRaw: skipping command because BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)   joint  1  is not in VOCAB_CM_POSITION_DIRECT mode
[ERROR] setReferenceRaw: skipping command because BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)   joint  1  is not in VOCAB_CM_POSITION_DIRECT mode
[ERROR] setReferenceRaw: skipping command because BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)   joint  1  is not in VOCAB_CM_POSITION_DIRECT mode
[ERROR] setReferenceRaw: skipping command because BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)   joint  1  is not in VOCAB_CM_POSITION_DIRECT mode
[ERROR] setReferenceRaw: skipping command because BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)   joint  1  is not in VOCAB_CM_POSITION_DIRECT mode
[ERROR] |event-downsampler| [mc.skipped-cmd-wrong-mode] BOARD right_arm-eb3-j2_3 (IP 10.0.1.3)  - detected 58 events on aggregate since the last message

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@github-actions github-actions bot changed the title Right Arm Elbow Encoder Reading Wrong Values ergoCub 1.1 S/N:001 – Right Arm Elbow Encoder Reading Wrong Values May 14, 2024
@github-actions github-actions bot added the ergoCub 1.1 S/N:001 ergoCub1.1 platform label May 14, 2024
@AntonioConsilvio
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Hi! @AntonioAzocar and I fixed both LCORE5 (RA_E3) cable and AMO cable (RA_S3). The robot has been tested and it works properly now! Closing!

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ergoCub 1.1 S/N:001 ergoCub1.1 platform
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